JETURBO ...JD TUNING ADELAIDE... Gold Donating Members 23,708 Member For: 16y 8m 7d Gender: Male Location: Adelaide Posted 23/08/14 05:02 AM Share Posted 23/08/14 05:02 AM From a fair wack of experiance with turbosmart actuators ( 7&12 psi ) you need far less preload than garrett actuators as they are strong springed items even though all "rated" actuators should perform as listed You can quite easily blow into 18-20 psi territory with initial desired boost levels Also not all turbosmart actuators are equal but this is another story, in the end we strongly suggest and used genuine garrett actuators for repeatability and end results Gunna I feel u need to bite the bullet and go for the tune shop of choice to Supply and fit an actuator RetuneThen sell off the turbosmart one .....This is about the best for your situation honestly 1 Link to comment Share on other sites More sharing options...
genuine honest person Member 2,769 Member For: 11y 10d Gender: Male Location: near brisbane Posted 23/08/14 05:49 AM Author Share Posted 23/08/14 05:49 AM that might be the case,lets see what the tuner says on monday when he runs it up on the dyno .but thanks for all the comments ,they do help .and they are appreciated ,no mater positive or negative I would love to hear them . Link to comment Share on other sites More sharing options...
Kosij Donating Members 2,045 Member For: 13y 5m 27d Gender: Male Posted 23/08/14 07:30 AM Share Posted 23/08/14 07:30 AM Was that first picture of the flapper shut and light coming in? Link to comment Share on other sites More sharing options...
genuine honest person Member 2,769 Member For: 11y 10d Gender: Male Location: near brisbane Posted 23/08/14 08:08 AM Author Share Posted 23/08/14 08:08 AM (edited) yes ,it is . joe at cms said it was ok to use ? if that is my problem there will be some not so pleasant phone calls coming up . Edited 23/08/14 08:19 AM by gunna Link to comment Share on other sites More sharing options...
Kosij Donating Members 2,045 Member For: 13y 5m 27d Gender: Male Posted 23/08/14 12:23 PM Share Posted 23/08/14 12:23 PM should seal 100%But that won't cause your issues maybe a tad bit of lag but nothing much.I would say refit actuator and retune 1 Link to comment Share on other sites More sharing options...
genuine honest person Member 2,769 Member For: 11y 10d Gender: Male Location: near brisbane Posted 23/08/14 12:26 PM Author Share Posted 23/08/14 12:26 PM thank god for that .I just did not feel like taking the turbo back of and getting another flapper done Link to comment Share on other sites More sharing options...
discostig Manual mode ________________________ All day, erryday Donating Members 13,798 Member For: 17y 2m 13d Gender: Male Location: Probably above atmospheric pressure Posted 24/08/14 03:36 AM Share Posted 24/08/14 03:36 AM Gunna I'm cheering for ya buddy, looking forward to when you get it all sorted out. Should be a ripper, I know because I have similar power to your engine when it was in the last car. Just wish I could help with what the problems are! 1 Link to comment Share on other sites More sharing options...
genuine honest person Member 2,769 Member For: 11y 10d Gender: Male Location: near brisbane Posted 24/08/14 05:19 AM Author Share Posted 24/08/14 05:19 AM thanks mate ,I will know more tomorrow . Link to comment Share on other sites More sharing options...
genuine honest person Member 2,769 Member For: 11y 10d Gender: Male Location: near brisbane Posted 25/08/14 07:19 AM Author Share Posted 25/08/14 07:19 AM (edited) well, they run it up on the dyno and it had 262 rwkw and 806 nm . They then phoned me and said that the 440 Bosch injectors were on there limit .They suggested to go to id 1000 .All I could say was just do it ,I want to see 310 rwkw . In the time that they waited for the injectors to arrive, they had a bit of a tune with it and ended up with about 290 rwkw .But they had lots of problems with low down boost fluctuating up and down (from 1000rpm to 3000 rpm ).They just could not work out what was wrong.After work I went and called in to see how it all was going . The worker that was changing the injectors then explained the problems they were facing . I then asked if it may be the flapper mod that I had done that did not seal 100%. His reply was that would certainly not help and thought that that may be why they are unable to tune it down low . To eliminate some problems I just asked him to change the actuator to a 12 psi f6 one ,and throw the turbosmart one in the bin.So in all fairness RDP had done a ok job to get it to where it was ,just would have been nice if they would have spend a bit of time diagnosing the car . I would have said just fix it Edited 25/08/14 07:26 AM by gunna Link to comment Share on other sites More sharing options...
pro346 Member 63 Member For: 12y 9m 27d Posted 25/08/14 07:21 AM Share Posted 25/08/14 07:21 AM Updates on this? hope you got it sorted today... Link to comment Share on other sites More sharing options...
Recommended Posts
Create an account or sign in to comment
You need to be a member in order to leave a comment
Create an account
Sign up for a new account in our community. It's easy!
Register a new accountSign in
Already have an account? Sign in here.
Sign In Now