grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 13/11/14 02:25 AM Author Share Posted 13/11/14 02:25 AM Just an update, Cooler and pipes, turbo side & battery relo swell as gauges all in, now just need to wait one month until I can get down to Melbourne for the rest. Link to comment Share on other sites More sharing options...
Bizkets is Drunk? Too heavy needs boost Member 5,929 Member For: 11y 3m 18d Gender: Male Location: Adelaide Posted 13/11/14 05:40 AM Share Posted 13/11/14 05:40 AM you know the rules. pics or didn't happen. 1 Link to comment Share on other sites More sharing options...
grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 13/11/14 08:46 AM Author Share Posted 13/11/14 08:46 AM (edited) Here is a few putting it all on and the one at the end, Excuse the snapchat text, only photos I got haha Edited 13/11/14 08:47 AM by grimie16 Link to comment Share on other sites More sharing options...
PTR_NITRO_FG Donating Members 3,214 Member For: 11y 5m 29d Gender: Male Location: NOR Perth Posted 13/11/14 12:31 PM Share Posted 13/11/14 12:31 PM What cooler? Plaz 800hp or 1000hp?Assume its plaz turbo side & battery relo? Looks good mate! Link to comment Share on other sites More sharing options...
grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 13/11/14 09:39 PM Author Share Posted 13/11/14 09:39 PM 800hp Mate Bit of cutting needed to be done but a lot more stuffing around with the 1000hp, that's bait overkill for what I need anyway hahaAnd yea plaz battery relo and turbo side.If I had my time again though I would go the pw unit and make my own turbo side and battery relo. I've heard from a few people how easy they are to make, but once I actually pulled it out of the box I saw how basic it was, but ah well. I also hadn't seen ratters comparison between the PW 1 (Which requires no cutting) and the plaz 2 until after I bought everything. PW 1 is as good if not better according to the paper, still both great brands for what I'll be doing anyway. Cheers mate 1 Link to comment Share on other sites More sharing options...
grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 06/12/14 01:03 AM Author Share Posted 06/12/14 01:03 AM So, Just encountered my first problem, Was driving along the highway, went to put my foot down and noticed I had lost all boost. Vacuum was and still is as normal as ever just won't get above 0psi, no warning lights, was not over boosting, everything still looks normal under the bonnet, all piping still connected and all and sounds fine revving up until 2500 rpm in neutral. Any ideas? Link to comment Share on other sites More sharing options...
MattyP MattyP Cruise Control 6,317 Member For: 12y 6m 20d Gender: Male Location: Central Coast Posted 06/12/14 01:30 AM Share Posted 06/12/14 01:30 AM Throttle body elbow popped off or leak in piping from turbo to throttle body or waste gate failing to close Link to comment Share on other sites More sharing options...
grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 06/12/14 01:45 AM Author Share Posted 06/12/14 01:45 AM Found it, hose clamp on the cold side of cooler had come loose, first time I looked pipe hadn't come off but I missed the clamp, now it's completely off, thank god it is only that 1 week out of the tune haha Link to comment Share on other sites More sharing options...
grimie16 Member 45 Member For: 10y 3m 10d Gender: Male Location: ACT Posted 27/12/14 02:30 AM Author Share Posted 27/12/14 02:30 AM So a bit of a delay in posting about the updates, but finally everything is done. After a drive from Canberra down to Melbourne I was set to get this all wrapped up. I showed up about half an hour to early at Pitlane (was a little bit excited) in order to get everything under way at the time we set out. So the car was dropped off and I spent a day walking the streets of Frankston. I had to head down further south that night so I sorted out a little hire car to last me the night. Somehow, Mick was able to get everything we set out on doing done within the day (Thanks a lot if you're reading this). This meant I was able to piss away the little Getz me and the old man had hired to get ourselves further south that night thank god. I was stoked with the end result, as was Mick. We ended up with 310rwkw at 14psi which was exactly what I was hoping for and drives like a dream. Can't say enough about the quality of work that shop produces, the car is now tenfolds better. Pitlane as a shop were a level above in my opinion. There customer service is brilliant and they work on your car like it is there own. The enthusiasm down there surely reflects on the quality of work produced, and ensured me that my car wasn't a "Last week at work" job like the attitude of some other shops I dealt with. Thanks again to Mick and the team at Pitlane, would highly recommend, even if it is a bit of a drive. 8 hours was not a hassle for that quality of work. 1 Link to comment Share on other sites More sharing options...
PTR_NITRO_FG Donating Members 3,214 Member For: 11y 5m 29d Gender: Male Location: NOR Perth Posted 27/12/14 04:20 AM Share Posted 27/12/14 04:20 AM Well done mate! that's bloody dedication driving 8 hrs for a tune! Lol Did you end up getting a surge tank or upgraded intank at all? Link to comment Share on other sites More sharing options...
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