Ralph Wiggum Moar Powar Babeh Lifetime Members 19,323 Member For: 19y 1m 24d Gender: Male Location: Perth Posted 24/05/17 12:58 AM Share Posted 24/05/17 12:58 AM Those pads killed the caliper not the other way around. Link to comment Share on other sites More sharing options...
k31th less WHY; more WOT Site Developer 28,949 Member For: 16y 7m 6d Gender: Male Location: Melbourne Posted 24/05/17 01:01 AM Share Posted 24/05/17 01:01 AM probably... by just getting too low and allowing the piston to push out too far which stretched and made the dust boot fail at it's full length and that allowed dust into the piston which caused it to sieze? Link to comment Share on other sites More sharing options...
Ralph Wiggum Moar Powar Babeh Lifetime Members 19,323 Member For: 19y 1m 24d Gender: Male Location: Perth Posted 24/05/17 01:03 AM Share Posted 24/05/17 01:03 AM exactamundo, plus less pad material = more heat transfer to the piston/boot/seals and resulting in the above. There a reason why a "worn out" pad still has 3 to 5mm or material left. 1 Link to comment Share on other sites More sharing options...
k31th less WHY; more WOT Site Developer 28,949 Member For: 16y 7m 6d Gender: Male Location: Melbourne Posted 24/05/17 01:12 AM Share Posted 24/05/17 01:12 AM fair dinkum... I've changed pads with less meat on them without issue... perhaps I was just lucky on those occasions. Link to comment Share on other sites More sharing options...
Ralph Wiggum Moar Powar Babeh Lifetime Members 19,323 Member For: 19y 1m 24d Gender: Male Location: Perth Posted 24/05/17 02:13 AM Share Posted 24/05/17 02:13 AM (edited) In this pic it looks like the top of the disc isn't flush with the top of the pad? That patch of rotor that's not seeing any pad action is weird? Edited 24/05/17 02:14 AM by Ralph Wiggum Link to comment Share on other sites More sharing options...
k31th less WHY; more WOT Site Developer 28,949 Member For: 16y 7m 6d Gender: Male Location: Melbourne Posted 24/05/17 02:32 AM Share Posted 24/05/17 02:32 AM that's as far down as it goes... that pic is of the passenger side, the pic above it in my post is the driver side (the one that had the piston failure) and they both seem to have the same amount of disc usage percentage Link to comment Share on other sites More sharing options...
Uberxr New Member 9 Member For: 7y 11m 11d Posted 24/05/17 04:22 AM Share Posted 24/05/17 04:22 AM so after collie a few weeks ago, I developed the dreaded flex plate rattle, (not bad for 180k) so it was out with the box and time for an upgrade. it was time to take the turbo off as well and upgrade the wastegate. so after pulling the car apart I found a few things that needed attention, Flex plate needed to be replaced, gearbox rubber mount had sheered in half, turbo had something go through it, two studs were missing to the manifold, and the exhaust housing bolts were all loose. So I got the new flex plate reinforced and ordered a new mount for the gearbox, a good mate came to the rescue with a good condition stock turbo so that was pulled apart and mr wiggum set it up with a ported rear housing and Turbosmart 12lb actuator. (Thanks again mate) So it all went back together albeit a few hiccups (my fault rushing things) but it seems to be running sweet now. Ill put a few kms on it to make sure everything is all good, then it will get a retune. Link to comment Share on other sites More sharing options...
ScatterBrain Donating Members 316 Member For: 15y 5m 15d Gender: Male Location: Brisbane Posted 24/05/17 08:07 AM Share Posted 24/05/17 08:07 AM (edited) Finally finished the last of the oil cooler ducting, Hopefully no more overheating on the race track. Edited 24/05/17 08:07 AM by ScatterBrain 5 Link to comment Share on other sites More sharing options...
Puffwagon Puff Gold Donating Members 15,858 Member For: 9y 9m 18d Gender: Male Location: South Australia Posted 24/05/17 08:40 AM Share Posted 24/05/17 08:40 AM I didn't do much exciting to my car today. I found the fouled plug and tried to revive it but no luck so I chucked a spare in and all was good again. Link to comment Share on other sites More sharing options...
Ralph Wiggum Moar Powar Babeh Lifetime Members 19,323 Member For: 19y 1m 24d Gender: Male Location: Perth Posted 24/05/17 12:14 PM Share Posted 24/05/17 12:14 PM 4 hours ago, ScatterBrain said: Finally finished the last of the oil cooler ducting, Hopefully no more overheating on the race track. Pics of S369?? Link to comment Share on other sites More sharing options...
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