Jump to content

Recommended Posts

  • Member
  • Member For: 15y 8m 12d
  • Gender: Male

After having a good look around the engine bay I found the hose clamp that clamps the small rubber joiner @ the throttle body to the to the standard crossover to be totally loose as in never tightened up. I hope this is the reason he was having a hard time getting power out of it.. Only thing is it hasnt popped off the fitting. So I cant be sure its definatelty loosing boost through there, being 14psi I dont know if that would be enough to let air escape.

Is it possible that this could be contributing to the power drop I had when I got the car retuned?? I am taking it back to him on monday to get it checked out on the dyno after it is tightened up. It would give me gr8 peace of mind knowing this was the cause of the power drop and not the piston failing

  • Replies 25
  • Created
  • Last Reply

Top Posters In This Topic

  • Member
  • Member For: 15y 8m 12d
  • Gender: Male

did the tuner not tighten this up after doing the flapper mod?

Yeah mate spot on. I also noticed the dipstick bracket bolt wasnt tight either

Edited by Brendan XR6-T
  • Member
  • Member For: 15y 8m 12d
  • Gender: Male

One thing I forgot to add is there is a small weeping oil leak on the passenger side of the car toward the front of the motor between the head and the block. Although I have noticed this a while ago there really isnt that much oil there at all just like a residue dust collector. This obviously needs to be repaired but tuner reckons it is a very small amount of oil there and since its been there for a while its not worth repairing unless it gets any worse.

  • Member
  • Member For: 15y 8m 12d
  • Gender: Male

could be from between the timing cover and head or block.

Not totally with what your saying but it looks like its coming from where the head and block join together, starts approx. 1 inch from the front and goes for approx 3-4 inches towards the back.

  • Member
  • Member For: 15y 8m 12d
  • Gender: Male

Went back to the rollers today after everything was tight and retuned it pulled 310rwkw. Torque seems abit higher than before but for some annoying reason it was tuned in 3rd this time didnt realise till I got home. I dont know if it akes any difference tuning from 3rd to 4th some ppl say it does some say it doesnt after reading around for the last couple of hrs. All in all I took it back he was more than happy to retune it everyone makes mistakes car seems happy im happy.

The two attached dyno runs are not back to back. The 320rwkw was about 4-5months ago in 4th gear.

The other today in 3rd

320rwkw1.doc

310rwkw1.doc

Edited by Brendan XR6-T
  • Donating Members
  • Member For: 16y 11m 22d
  • Gender: Male
  • Location: brisbane

go get a second opinion at autotech, tunehouse or cv.

Edited by bluprinturbo
  • Donating Members
  • Member For: 16y 10m 19d
  • Gender: Male
  • Location: Gold Coast, QLD

320kw @ the rollers in third is the same as 320kw at the rollers in 4th... The power is being read at the back wheels. the car is still putting 320kw to the ground only some put the 330down while in 3rd gear, and others get it down in 4th gear.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now
  • Recently Browsing   0 members

    • No registered users viewing this page.



×
  • Create New...
'