simmo Member 431 Member For: 21y 11m 3d Gender: Male Location: byron bay more underarm hair per square km Posted 08/08/09 09:06 AM Share Posted 08/08/09 09:06 AM (edited) all of a sudden my car wont make much boost ive checked all the piping the car is running an edit and cooler at 10psi now all it makes is 3 psi and under load eventually gets to 5 psi.ive even gutted the cat as I thought it was the issue cause the car feels choked.today I rermoved the boost solenoid and sprayed it up with wd40 on the way home the car made a bit more boost it actually started to spike I also removed a code saying p1228 wastegate control system failed open which hasnt appeared before it seems to me that solenoid has failed anyone heard of this before p.s. I have heard of cleaning that solenoid to restore boost? any help would be welcomed . Edited 08/08/09 09:09 AM by simmo Link to comment Share on other sites More sharing options...
jacob_xr6turbo Donating Members 433 Member For: 17y 4m 1d Location: Richmond, Melbourne Posted 08/08/09 09:12 AM Share Posted 08/08/09 09:12 AM broken actuator (causes it to stay open and not make boost) faulty solenoid..could also be the impeller in the exhaust housing?? some other guy had a similar problem in another thread.. Link to comment Share on other sites More sharing options...
Adam Here since the start... Lifetime Members 10,282 Member For: 21y 8m 18d Gender: Male Location: Victoria Posted 08/08/09 10:31 AM Share Posted 08/08/09 10:31 AM It spiked because you've gutted the cat. Link to comment Share on other sites More sharing options...
simmo Member 431 Member For: 21y 11m 3d Gender: Male Location: byron bay more underarm hair per square km Posted 08/08/09 01:38 PM Author Share Posted 08/08/09 01:38 PM how can I tell if its the waste gate or boost solenoid,if it is the wastegate can I fit a 12psi one without having to port th turbo? Link to comment Share on other sites More sharing options...
PHANTMXR6 It's not a MKI! Member 1,742 Member For: 16y 6m 24d Gender: Male Location: Earth Posted 08/08/09 11:13 PM Share Posted 08/08/09 11:13 PM Disconnect the hose to the actuator and drive it.Just be careful as there will be no boost control. Link to comment Share on other sites More sharing options...
RAP1D Member Donating Members 3,739 Member For: 18y 7m 24d Gender: Male Location: Sydney NSW Posted 09/08/09 02:10 AM Share Posted 09/08/09 02:10 AM Get under it and see if the atuator rod has come off the wastegate arm... its held on with a circlip so might have just popped off, causing the wastegate to be open. Link to comment Share on other sites More sharing options...
dezzaxr6t Donating Members 86 Member For: 17y 5m 13d Gender: Male Location: Canberra, ACT Posted 31/08/09 10:31 AM Share Posted 31/08/09 10:31 AM Hey,Any out come on the issues with the Boost from the first post? As I’m having the same problem with mine at the moment! Running 14psi but only getting 9psi??? I have checked all piping/bolts etc? Plus one of the above posts says to disconnect the hose from under the Actuator??? If it boosts does that mean the Actuator is stuffed? Please excuse my stupidity on this subject!Thanks Derek Link to comment Share on other sites More sharing options...
ChoCCo Member 68 Member For: 16y 9m 29d Location: Melbourne, VIC Posted 01/09/09 03:24 AM Share Posted 01/09/09 03:24 AM I'm interested as well because im having similar problems to the first post...I've done;- Rapid's V2.0 cooler- Deleted centre muffler + hi-flow cat- Custom 10psi tune- Liquid LPG systemExcept mine is a little different. its a BA Mk1 Auto and thru first gear, it hits 10psi no problem but then once 2nd kicks in the boost drops to 4psi then jumps to 7psi and fluctuates for a bout 3-4 seconds then jumps up to 10psi again thru the rest of the gears.what my tuner told me is that it could be to do with the actuator or torque management kicking in reducing the boost to save the auto. also, the timing doesnt back off. but he reckons most likly its the torque management.in a couple weeks im changing the valve springs and a re-tune, I'll keep you guys posted with a verdict does anyone else know what it might be?also, on the Mk1's, whats the "safest" boost level I can run before I start breaking sh!t? Link to comment Share on other sites More sharing options...
dezzaxr6t Donating Members 86 Member For: 17y 5m 13d Gender: Male Location: Canberra, ACT Posted 11/09/09 06:49 AM Share Posted 11/09/09 06:49 AM Hey guys, thought I would let you know that we fixed my boost problem!It was the cat!!!! For some reason it was mounted in the dump pipe??? And it just broke away, which then stopped the flow of pressure! Well that's what I have been told anyway!!But all I can say is the car has never ran better! Now I have a stainless steel 1000hp high flow cat on the car! I just can't believe how much off a difference a stainless steel cat can make! Other then the high flow cat I had on before!Now just a retune and I will be very happy!!Derek Link to comment Share on other sites More sharing options...
Recommended Posts
Create an account or sign in to comment
You need to be a member in order to leave a comment
Create an account
Sign up for a new account in our community. It's easy!
Register a new accountSign in
Already have an account? Sign in here.
Sign In Now