Trough Lolly Member 4,349 Member For: 20y 5m 16d Gender: Male Location: Mildura Posted 27/05/09 02:50 PM Share Posted 27/05/09 02:50 PM christiaan, youve got nothing to worry about.Theres guys out there running ALOT more than 400rwkw on 60lb siemens and no problems, id say it was a bodgy injector or even a fuel pressure problem. Link to comment Share on other sites More sharing options...
Huffin6 Member 3 Member For: 17y 5m 24d Posted 28/05/09 12:12 PM Share Posted 28/05/09 12:12 PM Huffin, reason I asked, is that I just got a set of these injectors installed so I'm obviously a bit worried now..I'm running 300rwkw at 12psi, and the afr's are all good..Hopefully everything stays ok.If you have had it tuned tand run 300 RWKW I recon you would be okay, even better if your tuner supplied them, chances are he would have checked them. Link to comment Share on other sites More sharing options...
DesFlurane Member 351 Member For: 18y 10m 6d Gender: Male Posted 09/06/09 05:36 AM Author Share Posted 09/06/09 05:36 AM (edited) Head came off today and low and behold piston damage. No5 worse than No4 , only have good picture of No4.All the others look perfect.Also defect on No4 on the turbo side, No5 on the plenum side.Barrels slightly marked so should be good for a rebuild not a complete short. Edited 09/06/09 05:39 AM by DesFlurane Link to comment Share on other sites More sharing options...
cobrav8 Member 1,969 Member For: 19y 11m 1d Gender: Male Location: New Zealand Posted 10/06/09 03:23 AM Share Posted 10/06/09 03:23 AM So what caused the damage - a backfire under high boost?PS - did your PW bits arrive ok? Link to comment Share on other sites More sharing options...
DesFlurane Member 351 Member For: 18y 10m 6d Gender: Male Posted 10/06/09 06:18 AM Author Share Posted 10/06/09 06:18 AM Thanks Bevan, boxes have arrived at Robins.Had a run with no boost control, boost alarm went off and I think that it had a big rattle, then the next WOT run at the drags two weeks later got the smoke out the back.Cause of the lack of boost control was the pipe coming off the actuator. Link to comment Share on other sites More sharing options...
cobrav8 Member 1,969 Member For: 19y 11m 1d Gender: Male Location: New Zealand Posted 10/06/09 11:28 AM Share Posted 10/06/09 11:28 AM Cool mate.I take it you will be double clamping all the pipes and lockwiring them on next time?Best of luck with the build Link to comment Share on other sites More sharing options...
DesFlurane Member 351 Member For: 18y 10m 6d Gender: Male Posted 11/06/09 02:34 AM Author Share Posted 11/06/09 02:34 AM When Eastern had the car they cut the pipe to the actuator, they reconnected it by putting a tube between the ends, no clamps nothing, no wonder it came off. Link to comment Share on other sites More sharing options...
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