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Cat Blow Out


Alion

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  • Member
  • Member For: 17y 11d
  • Gender: Male
  • Location: Figtree, Wollongong, NSW, 2525

Well where to start, I guess on tuesday the 8/7/08, the car was taken in to be tuned up gain as it seemed to have lost all of it power. As a dinorun showed at a car show a month before, only making 287HP at the wheels (yes horse power). When the car was brought it was ment to be making about 340KW at the fly. So what went wrong?

Well thax to a good mate (the guy who is tuning the car) and a fellow XR6T owner he can be trusted. So back to tuesday 8/7/08, car was on the dino for a full day of tuning but strangely enough only making 8psi of boost, when they where tuning it for 15 after much pondering on what the problem was they found a somthing a little sus. a bolt off the manifold to the turbo was gone and the rest was lose! so they pulled it all off looked at it all and found that the manifold was now bent. Was then michained and the such like. was the end of the day so car was layed to rest to tomorrow. :dontknow:

Wednesday 9/7/08, car was to go back on the dino later that day after the car was put back together and everything checked they found the bolts holding the turbine housings together where losse! So apart came the turbo. Was inspected and checked with no damage was put back together and it was the end of the day. :bangcomputer:

Thursday 10/7/08 the baby was put back to 1 again and went on the dino later that day with it still only making 8psi they decided to change the actuater. They had already tested it to make sure it wasnt the problem but better to be safe then sorry they thought. But still no luck 8 psi max boost. Then again what do you know it was the end of the day. :icon_ford:

Friday 11/7/08 (today) they found the problem!!!!!!! :bowdown: they decided to check the intake and exhaust system (as the compression had been tested about 1 month ago and came up fine). Well the intake was good but the Cat had been blowen out into the system and was doing a great job at chokeing everything up. So there was so much back presure the max boost was 8psi. So now that I have a cat case with no cat it will be staying that way till I have the money to get a deicent one.

Just thought I would share my problem with the world and at least the problem is fixed now. I dont think I am going to get sloged for all the time that has gone into this. But I am still going to have to pay for the machineing a few other things. In total I think I came away with a bargen and the service is fantastice but these guys are know for it. They are nispro accreated and they will be getting a letter of apreaction. (but I think I might use spell checked for that) :buttrock:

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  • Mmmmm......BOOST
  • Member
  • Member For: 17y 11m 4d
  • Gender: Male
  • Location: central coast

mate if someone has done the right thing by you don't hesitate to say their name helps others know who's good ,I know we have site sponsors but not all off us have easy access to them

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  • Member
  • Member For: 17y 11d
  • Gender: Male
  • Location: Figtree, Wollongong, NSW, 2525

Yeh I would if I could remember there name. There in Cairns on Muir St down the end doesnt look like much from the outside.

I will repost when I remember there name sorry for that guys

Edited by Buf-Phoon
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  • Into the laaaake
  • Member
  • Member For: 17y 9m 18d
  • Gender: Male
  • Location: Nrth Qld

Sounds like Cape York Automotive in Federation St.

And mate, its called a Dynamometer or Dyno for short. And yes I do believe you need to run spell check on your entire post.

cape-york-1.jpg

Edited by hanra
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  • Member
  • Member For: 17y 11d
  • Gender: Male
  • Location: Figtree, Wollongong, NSW, 2525
Sounds like Cape York Automotive in Federation St.

And mate, its called a Dynamometer or Dyno for short. And yes I do believe you need to run spell check on your entire post.

Yes sorry it is Cape York Automotive in Federation Street. I am just lazy at the moment due to the flu. ill fix it now

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  • Member
  • Member For: 17y 11d
  • Gender: Male
  • Location: Figtree, Wollongong, NSW, 2525

Well doesnt look like I can edit the first post so here it is all again!

Well where to start, I guess on Tuesday the 8/7/08, the car was taken in to be tuned up gain as it seemed to have lost all of it power. As a dyno run showed at a car show a month before, only making 287HP at the wheels (yes horse power). When the car was brought it was suppose to be making about 340KW at the fly. So what went wrong?

Well thax to a good mate (the guy who is tuning the car) and a fellow XR6T owner he can be trusted. So back to Tuesday 8/7/08, car was on the dyno for a full day of tuning but strangely enough only making 8psi of boost, when they where tuning it for 15 after much pondering on what the problem was they found a something a little suspicious. A bolt off the manifold to the turbo was gone and the rest was loose! So they pulled it all off looked at it all and found that the manifold was now bent. Well that to be machined as it was the end of the day so car was laid to rest to tomorrow.

Wednesday 9/7/08, car was to go back on the dyno later that day after the car was put back together and everything checked they found the bolts holding the turbine housings together where loose! So apart came the turbo. Was inspected and checked with no damage was put back together and it was the end of the day.

Thursday 10/7/08 the baby was put back together again and went on the dyno later that day with it still only making 8psi they decided to change the actuator. They had already tested it to make sure it wasn’t the problem but better to be safe then sorry they thought. But still no luck 8psi max boost. Then again what do you know it was the end of the day.

Friday 11/7/08 (today) they found the problem!!!!!!! They decided to check the intake and exhaust system (as the compression had been tested about 1 month ago and came up fine). Well the intake was good but the Cat had been blown out into the exhaust system and was doing a great job at blocking everything up. So there was so much back pressure the max boost was 8psi. So now that I have a cat case with no cat it will be staying that way till I have the money to get a decent one.

Just thought I would share my problem with the world and at least the problem is fixed now. I don’t think I am going to get slogged for all the time that has gone into this. But I am still going to have to pay for the machining a few other things. In total I think I came away with a barge and the service is fantastic but these guys are known for it. They are Nispro accreted and they will be getting a letter of thanks.

Sorry if it was hard to read before I am a terrible speller and I got a lovely case of the flu.

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